Recent research progress on unstart mechanism, detection and control of hypersonic inlet

J Chang, N Li, K Xu, W Bao, D Yu - Progress in Aerospace Sciences, 2017 - Elsevier
The present paper aims to provide a summary report on recent research progress about
unstart mechanism, detection and control of hypersonic inlet to help the researchers working …

Unstart phenomena induced by flow choking in scramjet inlet-isolators

S Im, H Do - Progress in Aerospace Sciences, 2018 - Elsevier
A review of recent research outcomes in downstream flow choking-driven unstart is
presented. Unstart is a flow phenomenon at the inlet that severely reduces the air mass flow …

Control of supersonic inlet-isolator unstart using active and passive vortex generators

A Valdivia, KB Yuceil, JL Wagner, NT Clemens… - AIAA journal, 2014 - arc.aiaa.org
An experimental study was conducted to investigate the effects of ramp-type vortex
generators in a Wheeler doublet configuration, vortex generator jets, and their combination …

Numerical simulation of stable and unstable ram-mode operation of an axisymmetric ethylene-fueled inlet-isolator-combustor configuration

CA Hash, PM Drummond, JR Edwards, N Kato… - Combustion and …, 2022 - Elsevier
Large-eddy simulations of stable and unstable ramjet operational modes are presented for
an axisymmetric inlet-isolator-combustor configuration experimentally tested in the …

Shock train/boundary-layer interaction in rectangular isolators

JS Geerts, KH Yu - AIAA Journal, 2016 - arc.aiaa.org
Shock trains in rectangular isolators with inflow Mach number of 2.5 and ARs of 3.0 and 6.0
are investigated. Knowledge gained is used to propose a rectangular isolator modification to …

Research on intelligent active disturbance rejection control algorithm for shock train leading edge of dual-mode scramjet

S Liang, M Guo, Y Tian, J Le, W Song - Physics of Fluids, 2024 - pubs.aip.org
To prevent scramjet inlet unstart, stringent control over the shock train's leading edge in the
isolator is necessary. Therefore, this study proposes a fuel flow active control scheme …

Control of high subsonic cavity flow using plasma actuators

K Yugulis, S Hansford, JW Gregory, M Samimy - AIAA journal, 2014 - arc.aiaa.org
Localized arc filament plasma actuators were used to control pressure fluctuations in a
cavity with a depth of 12.7 mm and length-to-depth ratio of 4.86. The rear wall of the cavity is …

Isolator dynamics during unstart of a dual-mode scramjet

LP Riley, DV Gaitonde, MA Hagenmaier… - Journal of Propulsion …, 2018 - arc.aiaa.org
The phenomenology of unstart in a dual-mode ethylene-fueled scramjet is studied in the
presence of inflow distortion using carefully calibrated unsteady Reynolds-averaged Navier …

Closed-loop control of shock-train location in a combusting scramjet

L Vanstone, KE Hashemi, J Lingren… - Journal of Propulsion …, 2018 - arc.aiaa.org
This study demonstrates the closed-loop control of a shock-train location in the isolator of a
Mach 2.2 direct-connect dual-mode scramjet facility (US Air Force Research Laboratory …

Response of shock train to high-frequency fluctuating backpressure in an isolator

B Xiong, ZG Wang, XQ Fan, Y Wang - Journal of Propulsion and Power, 2017 - arc.aiaa.org
Schlieren images and unsteady pressure measurements were collected to explore the
response of a shock train to a high-frequency fluctuating backpressure in an isolator. High …